yondering
02-11-2010, 07:09 PM
Thanks to some inspiration from bearmn56’s lee slug modifications, and a donor mold from sargenv, I’ve been experimenting with some modifications to the Lee 1 oz 12 gauge slug mold, and here’s what I’ve come up with.
My goal was to increase the weight and improve the nose shape of this slug, while hopefully improving accuracy as well. Since this slug is intended for rifled barrels, the hollow base foster design (intended for smoothbores) seemed out of place. I started by grinding down the mold’s center pin, the “key drive” section, to make a mostly solid slug with ~ 1/8” of the key drive portion remaining. I fired a few, and found the wad wasn’t pressing up against the solid inner base of the slug, so there was still empty wasted space inside. I then ground the key drive section down to .070”. I have not fired these yet, but my intent is for the wad to form into the key drive shape, completely and evenly filling the empty cavities at the base of the slug with no wasted volume that could be filled with lead.
I’m not a big fan of the round nose design of this slug, so I wanted to give it a larger flat nose. Because it’s a nose pour design, and the center pin is a smaller diameter than the slug OD, I couldn’t grind a full diameter reamer to change the nose shape. I thought about grinding a D-reamer that would fit through the center pin hole, but started looking around for other tools on hand that would do the job.
To run a reamer in through the center pin hole in the mold, though, the mold would need some alignment pins. The ridge on the key drive center pin aligns the mold halves vertically, so without it in place, the 2 halves will be out of alignment. I solved this by installing a couple alignment pins like most traditional mold halves use. I used the shaft from a worn out dremel bit for the pin material. 2 holes were drilled through the mold blocks (while assembled), then the pins were pressed into the holes in one block. After enlarging the holes in the other block and using a countersink, it was ready for nose profile modifications.
First I tried a ˝” diameter countersink. This worked fine, and gave the slug a .40” meplat diameter, although it was hard to keep the countersink perfectly centered in the mold. This meplat was still smaller than I wanted though.
Looking around some more, I spotted my LE Wilson case deburring tool. Aha! The diameter of the deburring tool body is ~ .015” smaller than the center pin hole in the mold. Perfect! I chucked the tool up in my cordless drill and spun it slowly in the mold. This gave the slug a nice truncated cone shape, with a .450” meplat diameter. Final weight is right about 515gr, although this particular mold casts slugs a little shorter than others, so most molds with these same modifications would probably run 520-525 gr.
I’m hoping to try these this weekend or next, I’ll post a range report at some point.
Here are some pictures. Keep in mind this is a resurrection of a damaged mold, with lots of dings in the cavity edges and a detached key drive section, so it's not as clean as a new mold would be.
Center pin, key drive section ground to .070”. The key drive section and the lip around the base have been cleaned up a little on the belt grinder, so the key drive is smaller diameter than original.
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2956.jpg
Staking center pin back on bracket
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2961.jpg
L.E. Wilson deburring tool in cordless drill
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2946.jpg
Reaming the nose
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2951.jpg
Nose modifications complete. Notice alignment pins.
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2954.jpg
Re-assembled mold, ready to cast
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2932.jpg
Original Lee slug and “Improved” slug bases
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2974.jpg
Left to right: Lee original, ˝” countersink nose, deburring tool nose, Lyman 525gr slug
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2964.jpg
Meplat diameters: .310” original, .400” countersink, .450” deburring tool, .550” Lyman
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2981.jpg
My goal was to increase the weight and improve the nose shape of this slug, while hopefully improving accuracy as well. Since this slug is intended for rifled barrels, the hollow base foster design (intended for smoothbores) seemed out of place. I started by grinding down the mold’s center pin, the “key drive” section, to make a mostly solid slug with ~ 1/8” of the key drive portion remaining. I fired a few, and found the wad wasn’t pressing up against the solid inner base of the slug, so there was still empty wasted space inside. I then ground the key drive section down to .070”. I have not fired these yet, but my intent is for the wad to form into the key drive shape, completely and evenly filling the empty cavities at the base of the slug with no wasted volume that could be filled with lead.
I’m not a big fan of the round nose design of this slug, so I wanted to give it a larger flat nose. Because it’s a nose pour design, and the center pin is a smaller diameter than the slug OD, I couldn’t grind a full diameter reamer to change the nose shape. I thought about grinding a D-reamer that would fit through the center pin hole, but started looking around for other tools on hand that would do the job.
To run a reamer in through the center pin hole in the mold, though, the mold would need some alignment pins. The ridge on the key drive center pin aligns the mold halves vertically, so without it in place, the 2 halves will be out of alignment. I solved this by installing a couple alignment pins like most traditional mold halves use. I used the shaft from a worn out dremel bit for the pin material. 2 holes were drilled through the mold blocks (while assembled), then the pins were pressed into the holes in one block. After enlarging the holes in the other block and using a countersink, it was ready for nose profile modifications.
First I tried a ˝” diameter countersink. This worked fine, and gave the slug a .40” meplat diameter, although it was hard to keep the countersink perfectly centered in the mold. This meplat was still smaller than I wanted though.
Looking around some more, I spotted my LE Wilson case deburring tool. Aha! The diameter of the deburring tool body is ~ .015” smaller than the center pin hole in the mold. Perfect! I chucked the tool up in my cordless drill and spun it slowly in the mold. This gave the slug a nice truncated cone shape, with a .450” meplat diameter. Final weight is right about 515gr, although this particular mold casts slugs a little shorter than others, so most molds with these same modifications would probably run 520-525 gr.
I’m hoping to try these this weekend or next, I’ll post a range report at some point.
Here are some pictures. Keep in mind this is a resurrection of a damaged mold, with lots of dings in the cavity edges and a detached key drive section, so it's not as clean as a new mold would be.
Center pin, key drive section ground to .070”. The key drive section and the lip around the base have been cleaned up a little on the belt grinder, so the key drive is smaller diameter than original.
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2956.jpg
Staking center pin back on bracket
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2961.jpg
L.E. Wilson deburring tool in cordless drill
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2946.jpg
Reaming the nose
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2951.jpg
Nose modifications complete. Notice alignment pins.
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2954.jpg
Re-assembled mold, ready to cast
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2932.jpg
Original Lee slug and “Improved” slug bases
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2974.jpg
Left to right: Lee original, ˝” countersink nose, deburring tool nose, Lyman 525gr slug
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2964.jpg
Meplat diameters: .310” original, .400” countersink, .450” deburring tool, .550” Lyman
http://i24.photobucket.com/albums/c26/zthang43/molds/IMG_2981.jpg