Buckshot
08-11-2008, 04:20 AM
http://www.fototime.com/C7B62885781C4F6/standard.jpghttp://www.fototime.com/A5F10F07ABFBF64/standard.jpg
I made myself a set of soft jaws! :-) Big whoopee deal eh!? Crap it took long enough. I probably could have filed one out faster, but I got to use all the 'Stuff'. Seems like all I was doing was cranking the knee up and down, and the table back and forth. First I took some 1/2-13 allthread and tuned a 60* point on each in the lathe. Took the steel jaws off and screwed in the pointy dealies.
Crank the vise out of the way. I oughta write that "CTVOOTW" because I did that a lot :veryconfu. Put in a collet and TI holder and TI, then Cranked the vise back and touched the TI back and forth across the tip to find 'it', and zeroed the DRO, then cranked over to the other one and entered it as a referance point. Then CTVOOTW, took out the pointy dealies slapped in a couple parallels and laid the pieces of aluminum in and tightened the jawless jaws.
The I CTKD (Cranked the Knee Down), took out the TI holder and put in the new (o-boy, I get to use it) new intregal shank Albreckt chuck and center drill. Then CTKU and move the table over to the 0.0000" place and center drill. Then CTKD and put in the 1/2" drill bit and CTKU drilled the hole. Then CTKD and put in a .520 reamer for clearance, CTKU and reamed the hole. CTKD and replace the reamer with a counterdrill. CTKU and counterdrill the hole.
Anyway, you get the idea [smilie=w: Of course I was using the quill to do the drilling, reaming etc. After the first was counterbored, the 2nd had to be done. The 1/2-13 sockethead screws fit perfectly just like this was the real deal, ha!
After the jaws were in and the vise closed up on them I touched off the endmill to zero the DRO so I could crank in on the Y axis to indicate .750" + .1875" for the width of a jaw plus half of the 3/8" endmill. So I cranked in .9375" and danged if that bloody endmill wasn't too far over the middle! I backed up and did it another couple times and boy this had me really stymied. Then I decided to check how thick the aluminum was. AHA, it's 5/8" and not 3/4". Yeesh!
After that it was smooth sailing. Ran the quill down to cut a .125" deep slot, hit the powerfeed and lit up a smoke, I deserved it :bigsmyl2:
...................Buckshot
I made myself a set of soft jaws! :-) Big whoopee deal eh!? Crap it took long enough. I probably could have filed one out faster, but I got to use all the 'Stuff'. Seems like all I was doing was cranking the knee up and down, and the table back and forth. First I took some 1/2-13 allthread and tuned a 60* point on each in the lathe. Took the steel jaws off and screwed in the pointy dealies.
Crank the vise out of the way. I oughta write that "CTVOOTW" because I did that a lot :veryconfu. Put in a collet and TI holder and TI, then Cranked the vise back and touched the TI back and forth across the tip to find 'it', and zeroed the DRO, then cranked over to the other one and entered it as a referance point. Then CTVOOTW, took out the pointy dealies slapped in a couple parallels and laid the pieces of aluminum in and tightened the jawless jaws.
The I CTKD (Cranked the Knee Down), took out the TI holder and put in the new (o-boy, I get to use it) new intregal shank Albreckt chuck and center drill. Then CTKU and move the table over to the 0.0000" place and center drill. Then CTKD and put in the 1/2" drill bit and CTKU drilled the hole. Then CTKD and put in a .520 reamer for clearance, CTKU and reamed the hole. CTKD and replace the reamer with a counterdrill. CTKU and counterdrill the hole.
Anyway, you get the idea [smilie=w: Of course I was using the quill to do the drilling, reaming etc. After the first was counterbored, the 2nd had to be done. The 1/2-13 sockethead screws fit perfectly just like this was the real deal, ha!
After the jaws were in and the vise closed up on them I touched off the endmill to zero the DRO so I could crank in on the Y axis to indicate .750" + .1875" for the width of a jaw plus half of the 3/8" endmill. So I cranked in .9375" and danged if that bloody endmill wasn't too far over the middle! I backed up and did it another couple times and boy this had me really stymied. Then I decided to check how thick the aluminum was. AHA, it's 5/8" and not 3/4". Yeesh!
After that it was smooth sailing. Ran the quill down to cut a .125" deep slot, hit the powerfeed and lit up a smoke, I deserved it :bigsmyl2:
...................Buckshot