seaboltm
11-30-2014, 07:13 PM
I bought one of the new Lee 379-250 molds for my 38-55. On the first casting session, no problems.
Second casting session was different. Sprew plate screw would not stay in place. One of the alignment pins pushed out giving me many bad boolits. In fact, I got zero boolits during my second session.
So I used a punch to push the alignment pin back into place and went back for session 3. No bueno. The pin pushed out again and the sprew plate screw would not stay in place.
So, I did the following fixes:
1. I put the pin back into place, and then I took a 1/8" Starret punch, placed half of the punch on the aluminum and half over hanging the pin hole. A quick pop or two with a ball peen hammer and I was rewarded with a perfect stake. In fact, it was so easy I added a second stake to the pin and then added two to the other alignment pin even though it had yet to move (I wasn't taking any chances.)
2. I keep 6-32 allen head set screws on hand, because well, they are handy. I also have the needed drill bits and 6-32 taps. So, I drilled a hole into the aluminum mold and into the sprew plate screw hole as shown in the pictures. Aluminum is easy to thread so that was simple.
Results: perfect. Those pins don't move, and there is really no way they can. And the sprew plate screw is now held securely in place.
Advice: don't over tighten the set screw as it is easy to strip aluminum. When staking the pins in place, go easy with the hammer. Aluminum is easy to move. Don't hit so hard as to move the pins deeper into the mold half. Just enough to barely touch.
This has probably been covered, but just in case I decided to post it. Oh, total repair time: 10 minutes.
Second casting session was different. Sprew plate screw would not stay in place. One of the alignment pins pushed out giving me many bad boolits. In fact, I got zero boolits during my second session.
So I used a punch to push the alignment pin back into place and went back for session 3. No bueno. The pin pushed out again and the sprew plate screw would not stay in place.
So, I did the following fixes:
1. I put the pin back into place, and then I took a 1/8" Starret punch, placed half of the punch on the aluminum and half over hanging the pin hole. A quick pop or two with a ball peen hammer and I was rewarded with a perfect stake. In fact, it was so easy I added a second stake to the pin and then added two to the other alignment pin even though it had yet to move (I wasn't taking any chances.)
2. I keep 6-32 allen head set screws on hand, because well, they are handy. I also have the needed drill bits and 6-32 taps. So, I drilled a hole into the aluminum mold and into the sprew plate screw hole as shown in the pictures. Aluminum is easy to thread so that was simple.
Results: perfect. Those pins don't move, and there is really no way they can. And the sprew plate screw is now held securely in place.
Advice: don't over tighten the set screw as it is easy to strip aluminum. When staking the pins in place, go easy with the hammer. Aluminum is easy to move. Don't hit so hard as to move the pins deeper into the mold half. Just enough to barely touch.
This has probably been covered, but just in case I decided to post it. Oh, total repair time: 10 minutes.