Lead melter
02-13-2008, 08:25 PM
In an attempt to increase the diameter of some 38-55 boolits, I beagled my Lee .379-250-RN/FP. The H&R I have will not shoot anything smaller than .379, and I hoped to get a little more diameter to possibly drive them a bit faster. Beagled boolits dropped out at .380-.382 depending on where they are measured. I used a harder mixture than normal, 1 part 20:1 and 1 part monotype, to try to get all the diameter I could. Lubed with LLA, as I have no sizer for this diameter.
Loaded the boolits in reformed 30-30 Win cases and kept OAL to 2.470". As I was seating them, I had a few boolits stick in the seating die, and also had a few that seated a lot deeper. Yes, I was crimping at that step as well. My first thought was that my seating plug had gotten fouled with dried LLA and stuck in place, so it was removed and no LLA found to cause problems on the plug, or in the die.
Reset the die back in the press, adjusted the seating plug on a properly seated cartridge and proceeded. After 2 or 3 more press strokes the same problem arose again.
Removed the seating plug again and found the boolit sticking in the roll crimp ring of the die. A slight tap with a pencil knocked it out, but there is obviously a problem somewhere.
I started looking at the seating die, and there in clear engraving is ."375" diameter. My 38-55 die has the same seating tolerences as the 375 Winchester. As near as I can figure, the larger diameter of the beagled boolit was just enough to catch on the crimp ring, as none of the .379" boolits gave any real problem.
Now, I plan to shoot these tomorrow to evaluate their worth, and if they are found to do better than the .379", I must address this problem in some way.
My first thought would be to enlarge the crimp ring diameter slightly. Having no access to a lathe, this presents a problem. So, I'm thinking maybe a 1/4" dowel rod with 1200 grit or crocus cloth wrapped around it. Give it a few dozen slow turns and try again?
Opinions and ideas are welcome.
Loaded the boolits in reformed 30-30 Win cases and kept OAL to 2.470". As I was seating them, I had a few boolits stick in the seating die, and also had a few that seated a lot deeper. Yes, I was crimping at that step as well. My first thought was that my seating plug had gotten fouled with dried LLA and stuck in place, so it was removed and no LLA found to cause problems on the plug, or in the die.
Reset the die back in the press, adjusted the seating plug on a properly seated cartridge and proceeded. After 2 or 3 more press strokes the same problem arose again.
Removed the seating plug again and found the boolit sticking in the roll crimp ring of the die. A slight tap with a pencil knocked it out, but there is obviously a problem somewhere.
I started looking at the seating die, and there in clear engraving is ."375" diameter. My 38-55 die has the same seating tolerences as the 375 Winchester. As near as I can figure, the larger diameter of the beagled boolit was just enough to catch on the crimp ring, as none of the .379" boolits gave any real problem.
Now, I plan to shoot these tomorrow to evaluate their worth, and if they are found to do better than the .379", I must address this problem in some way.
My first thought would be to enlarge the crimp ring diameter slightly. Having no access to a lathe, this presents a problem. So, I'm thinking maybe a 1/4" dowel rod with 1200 grit or crocus cloth wrapped around it. Give it a few dozen slow turns and try again?
Opinions and ideas are welcome.