Linstrum
07-22-2007, 08:27 AM
About two years ago I got a new Jet 13-inch swing by 40-inch gap bed lathe to replace the old Atlas lathe I had just shy of 50 years and wore out. My new lathe is a South Bend clone, so there are some pretty major differences between the two. When I got my new lathe out of the crate I checked it over for loose bolts, being lubed, plus other things like that, and I was really annoyed when :confused: I found that both the headstock and tailstock had never been tightened down sufficiently at the factory and the accuracy that had been painstakingly set by the factory technicians had all been lost!
:violin:
My first test cut produced a 2/1000” taper on a cut one inch long, which translates to 24/1000” per foot, pretty darned bad! So I got a 1.5-inch diameter bar of hot rolled steel about three feet long and chucked it up to start the alignment procedure. It is a must to sharpen the tool bit before beginning! Basically all it takes is common sense to adjust a lathe, a cut is taken up close to the headstock and the cross feed zeroed for that cut. Then the carriage is run down the bed about 10 inches and another cut made, with the final pass done with the cross feed at the same zero mark so the two cuts will hopefully be the same diameter. It takes a bit of finesse to make the two cuts so they are equal as the bar cannot be supported with the tailstock during this procedure since the alignment of the headstock with the bed is what is being checked and using the tailstock will prevent that. The natural flex of 10-inches of unsupported bar, lathe rpm, and the sharpness of the tool bit will all affect the depths of the two test cuts. Usually with the cross feed set at the zero point, three or four passes with a sharp tool bit at very slow rpm to avoid chattering at ten inches out from the chuck is good enough to make these test cuts on mild steel. If the two cuts are the same diameter then the lathe bed is on the same axis as the head stock axis. When they aren’t, the headstock is adjusted a tiny amount and then re-tightened down HARD, and then a light test cut is made at the same two points. When the two diameters match, that job is done. The next part of the job is to center the tailstock since the headstock was just moved, albeit just slightly. A shorter bar of scrap steel is mounted up between centers (don’t forget to take a truing-up cut on the center in the lathe chuck) and then a test cut is made and the bar checked for taper. Adjust the tailstock until there is no taper on the test bar, and when that is accomplished you are done. Don’t forget like the guy did who adjusted my lathe and forget to tighten things down! In fact, the test cuts MUST be done with everything as tight as they can get since tightening things up will often change the settings!
I had to adjust my lathe headstock twice, not long after doing it the first time I was making a very heavy cut that began to chatter violently and it knocked the headstock right back out of alignment. After the second time I adjusted it I also tightened down the headstock adjustment stop bolts as well to prevent sliding to the side and it has behaved itself since.
My latest job is machining a barrel for a .50 rifle :castmine: :cbpour: and in preparation for milling 26 inches of the 30-inch long barrel into an octagon measuring 1-1/2” across the flats, I trued up the barrel diameter between centers so it would be straight and parallel. After making the final 26-inch long cut I checked the barrel diameter and found that it measured 1.6004” at one end and 1.6000” at the other with an even taper down it of 4/10,000 of an inch! I’m not going to even think about fussing with that since getting a part machined to within 4/10,000” is quite often difficult at 12 inches length due to uneven heat treat hardness of many steel bars. :twisted:
It is nice to have a really good lathe! :drinks:
:violin:
My first test cut produced a 2/1000” taper on a cut one inch long, which translates to 24/1000” per foot, pretty darned bad! So I got a 1.5-inch diameter bar of hot rolled steel about three feet long and chucked it up to start the alignment procedure. It is a must to sharpen the tool bit before beginning! Basically all it takes is common sense to adjust a lathe, a cut is taken up close to the headstock and the cross feed zeroed for that cut. Then the carriage is run down the bed about 10 inches and another cut made, with the final pass done with the cross feed at the same zero mark so the two cuts will hopefully be the same diameter. It takes a bit of finesse to make the two cuts so they are equal as the bar cannot be supported with the tailstock during this procedure since the alignment of the headstock with the bed is what is being checked and using the tailstock will prevent that. The natural flex of 10-inches of unsupported bar, lathe rpm, and the sharpness of the tool bit will all affect the depths of the two test cuts. Usually with the cross feed set at the zero point, three or four passes with a sharp tool bit at very slow rpm to avoid chattering at ten inches out from the chuck is good enough to make these test cuts on mild steel. If the two cuts are the same diameter then the lathe bed is on the same axis as the head stock axis. When they aren’t, the headstock is adjusted a tiny amount and then re-tightened down HARD, and then a light test cut is made at the same two points. When the two diameters match, that job is done. The next part of the job is to center the tailstock since the headstock was just moved, albeit just slightly. A shorter bar of scrap steel is mounted up between centers (don’t forget to take a truing-up cut on the center in the lathe chuck) and then a test cut is made and the bar checked for taper. Adjust the tailstock until there is no taper on the test bar, and when that is accomplished you are done. Don’t forget like the guy did who adjusted my lathe and forget to tighten things down! In fact, the test cuts MUST be done with everything as tight as they can get since tightening things up will often change the settings!
I had to adjust my lathe headstock twice, not long after doing it the first time I was making a very heavy cut that began to chatter violently and it knocked the headstock right back out of alignment. After the second time I adjusted it I also tightened down the headstock adjustment stop bolts as well to prevent sliding to the side and it has behaved itself since.
My latest job is machining a barrel for a .50 rifle :castmine: :cbpour: and in preparation for milling 26 inches of the 30-inch long barrel into an octagon measuring 1-1/2” across the flats, I trued up the barrel diameter between centers so it would be straight and parallel. After making the final 26-inch long cut I checked the barrel diameter and found that it measured 1.6004” at one end and 1.6000” at the other with an even taper down it of 4/10,000 of an inch! I’m not going to even think about fussing with that since getting a part machined to within 4/10,000” is quite often difficult at 12 inches length due to uneven heat treat hardness of many steel bars. :twisted:
It is nice to have a really good lathe! :drinks: