44-henry
07-02-2011, 04:15 PM
Hello,
After watching lurking and reading a lot of old posts I decided to take a stab at making a mold. I have been playing around with an older TC Contender in 30 Herrett and I have been using Hornady 130 grain spitzers out of it with good success. Unfortunately the cost of bullets has made it kind of spendy to go on with this so I thought it might be worth seeing what a paper patch bullet would do.
Please keep in mind that this is my first venture into paper patching and mold making so I am a rank amateur at this and a lot of my methods are probably not the greatest. But I thought some of you might get a kick out of seeing the way I did it and hopefully can offer some suggestions to make the job easier, or more effective. Also, my bullet design is probably flawed and I realize that the nose is probably going to be too weak, but I made a couple extra cherries in other styles so if it doesn't work I will have some others that I can fall back on. In any event this was my strategy.
I wanted to make a D reamer so I started off by centering short length of 3/8" water hardening steel in my Sherline lathe using a dial indicator and a four jaw chuck.
http://img.photobucket.com/albums/v733/44-henry/SherlineLathe.jpg
I adjusted it until I had very little movement on the indicator, something under .001. I have access to much larger lathes, but the Sherline works nice for small stuff and the spindle speeds are much higher than on the other lathes. Once everything was dialed in I started turning down the blank. I was shooting for a diameter of about .303 at this stage and planned on reducing it down to .302 in finishing operations.
http://img.photobucket.com/albums/v733/44-henry/SherlineLatheFirstCut.jpg
Once my target diameter was reached I moved the head on the Sherline for a taper cut. This is the only easy way to cut tapers on the Sherline as it does not have either a compound slide, or an off settable tailstock. I actually have come to like this feature.
http://img.photobucket.com/albums/v733/44-henry/SherlineLatheTaperCut.jpg
Once the taper was set at about 14 degrees I proceeded to shape the nose of the blank. I actually adjusted the taper a couple different times to keep the nose concentric. When I was finished I smoothed out the steps with a fine cut file and than polished the blank with a progression of wet and dry sandpaper ending at 400 grit and backed with a steel parallel bar.
http://img.photobucket.com/albums/v733/44-henry/SherlineLatheFinishedProfile.jpg
My finished blank diameter was .302 at the base.
I wanted to avoid warpage as much as possible so I hardened the cherry next. I used a simple hand held propane torch and heated the cherry as evenly as possible inline with the flame. I don't have photos of this step since I was alone, but I used a magnet to check the temperature. When the magnet was no longer attracted I heated it a bit longer and than quenched. I quenched in cold water and tested with a file to ensure that it was hard. This is the cherry after hardening.
http://img.photobucket.com/albums/v733/44-henry/CherryAfterHardening.jpg
After hardening the cherry went back in the lathe for polishing and this is what it looked like after that step.
http://img.photobucket.com/albums/v733/44-henry/CherryAfterPolishing.jpg
Following this I again went with the seat of my pants approach and tempered the cherry with a small flame from the propane torch. I was shooting for a light straw color along the length of the cherry moving to a deep straw, purple color further back.
http://img.photobucket.com/albums/v733/44-henry/CherryAfterTempering.jpg
Once this was accomplished I placed the cherry in a small vise and attached this to the magnetic table of the surface grinder. I carefully ground the cherry to a thickness of .151. Following this I stoned the cherry on a fine oil stone and set it aside.
http://img.photobucket.com/albums/v733/44-henry/SurfaceGrinder.jpg
I next chucked a piece of 1" bronze bar stock in a another lathe and proceeded to turn down the diameter to .980 and face the ends. I than used a series of step drills to rough out the bulk of the cavity. I placed the cherry in the tailstock and set the lathe into reverse. With the spindle speed at about 60 rpm I proceeded to ream out the cavity. I would turn the tailstock hand wheel one full turn and than back the cherry out and clean the cavity with compressed air and brush off the chips from the reamer. I have heard some don't recommend cutting oil with bronze, but I used it anyways and it seemed to help. After a considerable amount of time the cavity was cut.
http://img.photobucket.com/albums/v733/44-henry/Reaming.jpg
I got sloppy and didn't record the next few operations, but here is what I did. I thoroughly cleaned out the cavity with alcohol and than proceeded to soot the interior. Next I cast several boolits in the unfinished mold and selected the best one. I was using Linotype for this step as I figured it would shrink less. As I had not fitted a sprue cutter I simply left a puddle and knocked the boolits out. I than took the test boolit and installed it in the three jaw chuck on my lathe and proceeded to face the base off. I than center drilled and tapped it for a 5-40 tap and left the tap in place as a handle. Next I used a fine valve grinding compound and liberally coated my lap with this and than worked it in the cavity with water as a lubricant and with the aid of a cordless hand drill. I would lap for awhile, clean the cavity, re-cast, and make a new lap. Eventually I ended up with a cavity that was smooth and consistent and would drop a boolit with little effort. The final boolits drop out of the cavity at .304.
http://img.photobucket.com/albums/v733/44-henry/TestBullet.jpg
I still need to add a sprue cutter and handle on the mold. Right now I am just using a set of old vise grips. I plan on facing the mold down so that it will drop a boolit that weighs in at about 130 grains. I will be making a push through sizing die to size this boolit down to .302, but I haven't had a chance to do that yet. I also gave some thought to making an ejector pin for the mold. At this point I decided against it since the boolits are coming out easily on their own. I also worry that the ejector pin might be a source of trouble down the road, but I am open to hearing opinions about that matter.
In any event it was fun and I learned a lot in the process. If you have any comments I would greatly appreciate hearing from you.
After watching lurking and reading a lot of old posts I decided to take a stab at making a mold. I have been playing around with an older TC Contender in 30 Herrett and I have been using Hornady 130 grain spitzers out of it with good success. Unfortunately the cost of bullets has made it kind of spendy to go on with this so I thought it might be worth seeing what a paper patch bullet would do.
Please keep in mind that this is my first venture into paper patching and mold making so I am a rank amateur at this and a lot of my methods are probably not the greatest. But I thought some of you might get a kick out of seeing the way I did it and hopefully can offer some suggestions to make the job easier, or more effective. Also, my bullet design is probably flawed and I realize that the nose is probably going to be too weak, but I made a couple extra cherries in other styles so if it doesn't work I will have some others that I can fall back on. In any event this was my strategy.
I wanted to make a D reamer so I started off by centering short length of 3/8" water hardening steel in my Sherline lathe using a dial indicator and a four jaw chuck.
http://img.photobucket.com/albums/v733/44-henry/SherlineLathe.jpg
I adjusted it until I had very little movement on the indicator, something under .001. I have access to much larger lathes, but the Sherline works nice for small stuff and the spindle speeds are much higher than on the other lathes. Once everything was dialed in I started turning down the blank. I was shooting for a diameter of about .303 at this stage and planned on reducing it down to .302 in finishing operations.
http://img.photobucket.com/albums/v733/44-henry/SherlineLatheFirstCut.jpg
Once my target diameter was reached I moved the head on the Sherline for a taper cut. This is the only easy way to cut tapers on the Sherline as it does not have either a compound slide, or an off settable tailstock. I actually have come to like this feature.
http://img.photobucket.com/albums/v733/44-henry/SherlineLatheTaperCut.jpg
Once the taper was set at about 14 degrees I proceeded to shape the nose of the blank. I actually adjusted the taper a couple different times to keep the nose concentric. When I was finished I smoothed out the steps with a fine cut file and than polished the blank with a progression of wet and dry sandpaper ending at 400 grit and backed with a steel parallel bar.
http://img.photobucket.com/albums/v733/44-henry/SherlineLatheFinishedProfile.jpg
My finished blank diameter was .302 at the base.
I wanted to avoid warpage as much as possible so I hardened the cherry next. I used a simple hand held propane torch and heated the cherry as evenly as possible inline with the flame. I don't have photos of this step since I was alone, but I used a magnet to check the temperature. When the magnet was no longer attracted I heated it a bit longer and than quenched. I quenched in cold water and tested with a file to ensure that it was hard. This is the cherry after hardening.
http://img.photobucket.com/albums/v733/44-henry/CherryAfterHardening.jpg
After hardening the cherry went back in the lathe for polishing and this is what it looked like after that step.
http://img.photobucket.com/albums/v733/44-henry/CherryAfterPolishing.jpg
Following this I again went with the seat of my pants approach and tempered the cherry with a small flame from the propane torch. I was shooting for a light straw color along the length of the cherry moving to a deep straw, purple color further back.
http://img.photobucket.com/albums/v733/44-henry/CherryAfterTempering.jpg
Once this was accomplished I placed the cherry in a small vise and attached this to the magnetic table of the surface grinder. I carefully ground the cherry to a thickness of .151. Following this I stoned the cherry on a fine oil stone and set it aside.
http://img.photobucket.com/albums/v733/44-henry/SurfaceGrinder.jpg
I next chucked a piece of 1" bronze bar stock in a another lathe and proceeded to turn down the diameter to .980 and face the ends. I than used a series of step drills to rough out the bulk of the cavity. I placed the cherry in the tailstock and set the lathe into reverse. With the spindle speed at about 60 rpm I proceeded to ream out the cavity. I would turn the tailstock hand wheel one full turn and than back the cherry out and clean the cavity with compressed air and brush off the chips from the reamer. I have heard some don't recommend cutting oil with bronze, but I used it anyways and it seemed to help. After a considerable amount of time the cavity was cut.
http://img.photobucket.com/albums/v733/44-henry/Reaming.jpg
I got sloppy and didn't record the next few operations, but here is what I did. I thoroughly cleaned out the cavity with alcohol and than proceeded to soot the interior. Next I cast several boolits in the unfinished mold and selected the best one. I was using Linotype for this step as I figured it would shrink less. As I had not fitted a sprue cutter I simply left a puddle and knocked the boolits out. I than took the test boolit and installed it in the three jaw chuck on my lathe and proceeded to face the base off. I than center drilled and tapped it for a 5-40 tap and left the tap in place as a handle. Next I used a fine valve grinding compound and liberally coated my lap with this and than worked it in the cavity with water as a lubricant and with the aid of a cordless hand drill. I would lap for awhile, clean the cavity, re-cast, and make a new lap. Eventually I ended up with a cavity that was smooth and consistent and would drop a boolit with little effort. The final boolits drop out of the cavity at .304.
http://img.photobucket.com/albums/v733/44-henry/TestBullet.jpg
I still need to add a sprue cutter and handle on the mold. Right now I am just using a set of old vise grips. I plan on facing the mold down so that it will drop a boolit that weighs in at about 130 grains. I will be making a push through sizing die to size this boolit down to .302, but I haven't had a chance to do that yet. I also gave some thought to making an ejector pin for the mold. At this point I decided against it since the boolits are coming out easily on their own. I also worry that the ejector pin might be a source of trouble down the road, but I am open to hearing opinions about that matter.
In any event it was fun and I learned a lot in the process. If you have any comments I would greatly appreciate hearing from you.